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Type: Posts; User: z28dyson

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  1. Sorry for my absence, I ended up pulling my...

    Sorry for my absence, I ended up pulling my engine and finding all kinds of bad stuff. I had 2 slightly bent valves and had wiped out #3 and #4 cam bearings as well as a frigged up pickup tube o ring...
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    Just the tps needs to be unplugged. Key off...

    Just the tps needs to be unplugged. Key off unplug tps, key on for 30 seconds then key off and plug tps back in. That's how I lowered my counts.
  3. I found some of the russk idle files today but...

    I found some of the russk idle files today but couldn't get them to open for some reason Ill keep working on that. What I did do was reduce the braf closer to what it wants in my log which was around...
  4. Sorry for the confusion it is drive by cable. It...

    Sorry for the confusion it is drive by cable. It has a stock truck throttle body. I have a cheapo 92 but it wouldn't run worth a sh*t with it so I bought a good used stock tb. I just got another idle...
  5. i have been reading till my eye's hurt about the...

    i have been reading till my eye's hurt about the proportional and integral tables and I'm not sure how raising them made it not stall hahaha I had it a 2000 on the log on post #10 but it wouldn't hit...
  6. I found the misfire, #7 plug wire was barley...

    I found the misfire, #7 plug wire was barley hanging on so I swapped #7 with #1 plug and wire and misfires are gone. Thanks for catching that. I also got the high idle under check by lowering the...
  7. Here is the log and tune.

    Here is the log and tune.
  8. I just noticed something, In that log where the...

    I just noticed something, In that log where the stft was going crazy I had disabled the ltft in that tune. This time I left them enabled and they were in check. That may have had something to do with...
  9. Thanks for getting back to me. I had a chance to...

    Thanks for getting back to me. I had a chance to check every thing over and all was good on the wiring side for the o2 sensors. i did notice those were out of wack so i went back and watched all my...
  10. Again I tank you for the advice, I really...

    Again I tank you for the advice, I really appreciate it.
  11. so I loaded the ve and made the spark...

    so I loaded the ve and made the spark corrections. I'm still learning to navigate the scanner, I partially figured out the graph configurations but couldn't get it to hit any cells when i made the...
  12. Here is the tune with the original ve that was in...

    Here is the tune with the original ve that was in it I added 20% to the idle area. I also added 15 degrees to the underspeed spark, starting at 10 then i increased it to 15 I aslo made the low rpm...
  13. Thanks for the response. I will try some of those...

    Thanks for the response. I will try some of those changes this afternoon. I never noticed how flat that ve table was as I never looked at the 3d graph, I think I'll paste in the ve from the my...
  14. stalling out when returning to idle in park or gear

    Hi all, i am having a issue with my ls swapped 1984 z28 stalling when coming back to idle in park and in gear. It is a 4.8l with a sloppy stage 2 cam, pac 1218 springs with a speedmaster ls6 style...
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