Originally Posted by
twenglish1
Yeah definitely strange, felt like something was wrong for sure, either the 3-4-3-4 or 3-4-lock-unlock-lock. I tried a few things before finding that the 3-4 torque reduction was it, I had also tried reducing the TCC min and max PWM to 1% and 0%, I almost forgot that I didn't install the valve to disable TCC pwm control from the sonnax shift kit, wasn't sure if this was a feature I might have ended up wanting to use at some point, and it's easy enough to disable it in the trans calibration, my thought here was that it was briefly sending pressure to the TCC during the shift, so I tried removing the PWM signal all together. I'm just happy it doesn't seem like there is anything wrong with the transmission, did not want to pull it again, I already had to install it twice after the rebuild, I found the plastic spacer that goes between the pump and the reverse input drum while cleaning up after I installed, filled and test drove it, not sure if it would have caused problems or not, but wasnt going to take the chance, won't make that mistake again thats for sure! Hahaha