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Thread: 12mm CP3 Tuning....need some help with FCA

  1. #1
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    12mm CP3 Tuning....need some help with FCA

    Hi all,

    New to the forum and need some help tuning this Exergy 12mm CP3. Truck currently won't even drive...

    Datalog file and picture are attached of where my issue is happening with truck not moving and engine revved to ~1900rpm (just rebuilt the engine and put the larger pump on in the process).

    The issue is very consistent. For the first 25-30sec actual and desired rail pressure are fine and generally in line, but then there it starts to vary up and down as the actual FCA DC increases, and then around 1min 15sec into the run (again very consistent) the FCA DC maxes out and pump loses rail pressure.

    I've tried 28 different tune adjustments mainly in the mA duty cycle table and this is the best I've gotten it so far, but as soon as I try to drive I can't go past 5% throttle or it loses pump pressure and starts smoking. Stock pump on this tune ran perfect so nothing should need to be changed with the timing/rp/duration tables. This is also where I had the FCA base table with the stock pump, but going up or down on that table doesn't do anything for the issue. 18psi consistently measured at the lift pump for low pressure side. I do see where its consistently going into the misfire timing table, but not sure why and also don't see how that is currently impacting the fuel side of things.

    Any help or support is much appreciated....

    Thanks!
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  2. #2
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    What happens if you try a stock tune?
    Providing custom file mods for ?Diets? on Ram Cummins 6.7L 2010+
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  3. #3
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    Stock values it varies much worse and more movement on the actual FC DC. Here is a datalog from that: 12mm CP3 FCA Issues (Stock mA Values).JPG

  4. #4
    Advanced Tuner MAIDENCR's Avatar
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    you have a leak on high pressure side...connector tube....injector....relief valve on the rail
    And idling at 17mm3 is a bit off if pulse table is set correctly it should idle a 10mm3
    03 cummins,175% flux injectors,dual cp3,s467.7/83 1.00
    Nv5600 with valair triple disc clutch

  5. #5
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    No visible leaks at any of the high pressure connectors. I forgot to mention checks I?ve done there - I?ve tried swapping rail pressure sensors, removing the PRV return line (only a small drop of fuel on top of the PRV after doing the same run as the catalog), and retorqued connector tubes to 40 ft lbs with no movement on any of the nuts. The truck ran perfect before the engine rebuild on the fuel side of things and each connector tube went back to the same injector on install. If I can?t figure this tune out by later today, my plan is to swap the stock CP3 back in. If it runs fine, then it eliminates the possibility of leaking connector tubes.

  6. #6
    Advanced Tuner MAIDENCR's Avatar
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    There is a reason why tune ask for more pressure and the pressure keep dropping....if it doest "work" with stock setting there is an issue...put back stock cp3 and try again...post a log too
    03 cummins,175% flux injectors,dual cp3,s467.7/83 1.00
    Nv5600 with valair triple disc clutch

  7. #7
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    Swapping the CP3 now and will post an update shortly.

  8. #8
    Advanced Tuner MAIDENCR's Avatar
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    Got stock pump in??
    03 cummins,175% flux injectors,dual cp3,s467.7/83 1.00
    Nv5600 with valair triple disc clutch

  9. #9
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    Agreed sounds like a leak on high pressure side. Injector or injectors not seated quite right, rail relief valve, cascade valve. Being a new pump shouldn’t be a bad cascade valve though.
    Providing custom file mods for ?Diets? on Ram Cummins 6.7L 2010+
    Can discuss on Telegram @ https://t.me/+y2N6u2hoNkJkZmUx

  10. #10
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    Okay....so some updates. I swapped CP3s and the issue remained EXACTLY the same so that rules out the cascade valve and CP3 from the high pressure system. I reconfirmed once again lift pump pressure during the issue and it stays constant at 18psi the whole time with no variation. Also retested the PRV by drying it out and having someone video during the run. It both stayed dry and also didn't visually have any fluid coming out.

    So then I decided to go get new connector tubes before the local shop closed and replaced all of the connector tubes and torqued them to 44 ft lbs. The issue remained exactly the same STILL lol....so I tried one more thing which is take the Fluidampr off and flip the tone ring 180 degrees just to make sure I didn't have that flipped upside down when I did the engine swap (I had two new pins/holes from the full power kit on the old engine so that could've been a possibility in my mind). After doing that, the truck won't start at all so I eliminated that possibility and will flip it back in the morning.

    I have a hard time believing an injector would just start leaking so much that it can't hold rail pressure when it ran perfect on the fuel side before the rebuild. The injectors were only out of the truck for around a week during that process and both placed on and covered by lint free rags. I always follow the install specs and torque to spec and have never had an issue before this with not having one seated correctly. Wouldn't the connector tube just not even push and click in if it wasn't seated properly?

    Since the issue is so consistent with holding and matching rail pressure for the first 20sec or so and then starting to do small adjustments and then big adjustments to the FCA almost like clockwork, I feel like I have a wiring issue where something is not sending the proper feedback to the ECM and its trying to correct something that doesn't need to be corrected. So tomorrow in addition to flipping the timing ring back 180 degrees, I will be back probing each wire in the circuit to test for continuity while moving the harness around so see if I can find anything.

    Any other ideas/thoughts are much appreciated! This image is of the datalog post new connector tube install: 12mm CP3 FCA Issues (New Connector Tubes).JPG

  11. #11
    Advanced Tuner MAIDENCR's Avatar
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    Did you change something else from before rebuilt? In the tune? Post the tune too
    03 cummins,175% flux injectors,dual cp3,s467.7/83 1.00
    Nv5600 with valair triple disc clutch

  12. #12
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    No changes to the tune for the last almost 9 years since HP tuners came out and got it dialed in. Instead of jumping to a wiring signal conclusion I decided to just unplug the FCA and watch rail pressure. It went to max as expected and then dropped, which means it has to be mechanical. Once I get this thing running I do plan to get this thread back on track with dialing in the 12mm pump lol. I got some good information from Exergy on flow values vs. FCA DC and mA in the process of all of this. Here is the datalog of FCA unplugged:12mm CP3 FCA Issues (FCA Unplugged).JPG

  13. #13
    Advanced Tuner MAIDENCR's Avatar
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    post log instead of picture of it....

    conclusion maybe an injector
    03 cummins,175% flux injectors,dual cp3,s467.7/83 1.00
    Nv5600 with valair triple disc clutch

  14. #14
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    Quote Originally Posted by xDiesel03 View Post
    No changes to the tune for the last almost 9 years since HP tuners came out and got it dialed in. Instead of jumping to a wiring signal conclusion I decided to just unplug the FCA and watch rail pressure. It went to max as expected and then dropped, which means it has to be mechanical. Once I get this thing running I do plan to get this thread back on track with dialing in the 12mm pump lol. I got some good information from Exergy on flow values vs. FCA DC and mA in the process of all of this. Here is the datalog of FCA unplugged:12mm CP3 FCA Issues (FCA Unplugged).JPG
    Means you got a high pressure fuel side leak, should maintain rail pressure being pegged if there isn’t a leak on the high pressure side.
    Providing custom file mods for ?Diets? on Ram Cummins 6.7L 2010+
    Can discuss on Telegram @ https://t.me/+y2N6u2hoNkJkZmUx

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    Well I think I found my issue?I?ve never had this happen before but looks like I had two injectors that didn?t seat all the way.

    When I replaced the connector tubes I inspected the old ones for any rings or wear marks to indicate an injector not fully seated, but saw nothing at all. Previously I had the old Bosch style tubes and the new tubes from Cummins are a bright/stainless appearance and also apparently a softer material because when I removed those I found gouges on both the number 3 and 4 cylinder tube.

    I wish I had seen that before pulling all six of the injectors lol, but at least I know now. Going to inspect and see if there is a washer stuck in the bore or just wasn?t seated from being a new head. It?s a DJ stage 1 head but not sure if it was bought new or a reman so either thing could be a possibility. Out of 5-6 times I?ve had injectors out and in I?ve never had this happen.

  16. #16
    Advanced Tuner MAIDENCR's Avatar
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    Glad you may have found your issue...it was clearly an high pressure leak issue
    03 cummins,175% flux injectors,dual cp3,s467.7/83 1.00
    Nv5600 with valair triple disc clutch

  17. #17
    Advanced Tuner MAIDENCR's Avatar
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    Got your leak fixed??
    03 cummins,175% flux injectors,dual cp3,s467.7/83 1.00
    Nv5600 with valair triple disc clutch

  18. #18
    Advanced Tuner MAIDENCR's Avatar
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    So???
    03 cummins,175% flux injectors,dual cp3,s467.7/83 1.00
    Nv5600 with valair triple disc clutch