So I been on this thing for hours and having issues with the timing being way higher than commanded. Luckily the knock sensors are doing their job and bringing it down but I've zero'd out everything in advance and logging every single advance PID. I've messed with driver demand and torque management as well as Virtual Torque and can't seem to get this thing dialed in! Wide open afr is hitting on target 12.5 / .85 however I had to put crazy numbers in the PE table to get there. I'm new to this platform so any help in the right direction would be awesome! Log / Tune attached.