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Thread: High LTFT 25%

  1. #1
    Potential Tuner
    Join Date
    Sep 2021
    Posts
    1

    High LTFT 25%

    Hello all I recently replaced a motor in a 2000 Pontiac Firebird WS6 it a stock replacement pulled from another one that was in a wreck, I have put BBK longtube headers on it deleted EGR and A.I.R. along with the Cats and rear o2 sensors motor has new spark plugs, new plug wires and a fresh oil change. After getting this done hooked up the VCM Scanner and my Bank 1 LTFT is reading at 25% and is showing it being rich and lean but will go away around 2k RPM, after searching the internet I came up with a few post saying it may be a bad o2 sensor or the connector also could be a vacuum leak I've done my due diligence on both of the scenarios with no resolution, I will attach the VCM scanner log as well any help is greatly appreciated.

    Thanks
    Charlie B.
    Attached Files Attached Files

  2. #2
    Advanced Tuner
    Join Date
    Mar 2020
    Posts
    380
    You most likely have an air leak. If not the intake, then pre o2 on bank one exhaust sucking fresh air in across the o2 causing a false lean reading
    Last edited by village_idiot; 09-17-2021 at 12:23 AM.